Go-Tech Engines Thread
#4472
#4473
Help
I have a gen5 7port that now has about 2 gallons on it and it screams. I started to see some high temps 315+ and took the motor apart. I noticed the carb sleeve had a tick or wiggle. I then replaced the carb with an OS vspec carb that a friend had. This immediately fixed both tuning and temp problems and the motor runs really well. However, recently I have been blowing plugs after approx 3-4 tanks of running. I thought maybe I was too lean but I have a smoke trail and am temping at 180-210max. I had been using P3 plugs then tried P4 plugs and right now I am trying P6 plugs. I am running odonnel 30% and have 1 copper shim and 1 alum shim. I also sealed up the motor with blue rtv and have installed a brand new tank. I am not sure where to go from here.
Help
Dan
I have a gen5 7port that now has about 2 gallons on it and it screams. I started to see some high temps 315+ and took the motor apart. I noticed the carb sleeve had a tick or wiggle. I then replaced the carb with an OS vspec carb that a friend had. This immediately fixed both tuning and temp problems and the motor runs really well. However, recently I have been blowing plugs after approx 3-4 tanks of running. I thought maybe I was too lean but I have a smoke trail and am temping at 180-210max. I had been using P3 plugs then tried P4 plugs and right now I am trying P6 plugs. I am running odonnel 30% and have 1 copper shim and 1 alum shim. I also sealed up the motor with blue rtv and have installed a brand new tank. I am not sure where to go from here.
Help
Dan
#4475
Rex
#4477
it was rebuilt with a new gen 5 piston/sleeve/rod but like I said, after 3/4 of a gallon the bushing on the rod went out, the engine was running very good, temps around 220-240 but out of no where it just stopped and found the bushing in pieces 
who can I contact about this issue?

who can I contact about this issue?
#4478
#4479
Help
I have a gen5 7port that now has about 2 gallons on it and it screams. I started to see some high temps 315+ and took the motor apart. I noticed the carb sleeve had a tick or wiggle. I then replaced the carb with an OS vspec carb that a friend had. This immediately fixed both tuning and temp problems and the motor runs really well. However, recently I have been blowing plugs after approx 3-4 tanks of running. I thought maybe I was too lean but I have a smoke trail and am temping at 180-210max. I had been using P3 plugs then tried P4 plugs and right now I am trying P6 plugs. I am running odonnel 30% and have 1 copper shim and 1 alum shim. I also sealed up the motor with blue rtv and have installed a brand new tank. I am not sure where to go from here.
Help
Dan
I have a gen5 7port that now has about 2 gallons on it and it screams. I started to see some high temps 315+ and took the motor apart. I noticed the carb sleeve had a tick or wiggle. I then replaced the carb with an OS vspec carb that a friend had. This immediately fixed both tuning and temp problems and the motor runs really well. However, recently I have been blowing plugs after approx 3-4 tanks of running. I thought maybe I was too lean but I have a smoke trail and am temping at 180-210max. I had been using P3 plugs then tried P4 plugs and right now I am trying P6 plugs. I am running odonnel 30% and have 1 copper shim and 1 alum shim. I also sealed up the motor with blue rtv and have installed a brand new tank. I am not sure where to go from here.
Help
Dan
#4480
I have had it happen both times. I plugged the exhaust to kill the motor then it would not restart. Then the most recent one I was running on the track and noticed a decrease in power, then 3/4 of the way around the track, the car died and the plug was dead.
#4481
it was rebuilt with a new gen 5 piston/sleeve/rod but like I said, after 3/4 of a gallon the bushing on the rod went out, the engine was running very good, temps around 220-240 but out of no where it just stopped and found the bushing in pieces 
who can I contact about this issue?

who can I contact about this issue?
Rex
#4482
Thanks for the reply. I thought that 1 copper and 1 alum shim was 30%. If not, how much performance would I lose by adding another .1 shim? Would it even be noticable? Also if that is the case, is it worth running 30% and adding a shim or leaving it alone and running 20%. I don't know much about this stuff but I am slowly learning.
Thanks
Dan
Thanks
Dan
#4485
Thanks for the reply. I thought that 1 copper and 1 alum shim was 30%. If not, how much performance would I lose by adding another .1 shim? Would it even be noticable? Also if that is the case, is it worth running 30% and adding a shim or leaving it alone and running 20%. I don't know much about this stuff but I am slowly learning.
Thanks
Dan
Thanks
Dan



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