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I picked up a pre run 24 with a gallon or so on it from a buddy yesterday....I am putting it in a STRR and plan on using Dyn 86 pipe with a P4 (Trinnity 30% fuel). Is it safe to assume this will be a good starting point? He ran it with JP2, but I really am not a JP pipe fan (even though I have two of them). I also take it the factory needle settings are HSN flush, and LSN slightly in from flush?
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Originally Posted by AETRUGGYMAN
(Post 5937605)
i have a trinity 24.it ran graet for about a halve gallon.but the last couple weeks i have been fighty to tune it.with stock needle settings it is way lean on the bottom.i have to turn out the low speed needles about 12 hours.somthing popped up today.it wont stay running when you it the brakes.i am feed up with engines. i am going back dyn. xpthat ran a hole lot better.any help would be great.
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I found out today that I ended up with one of the EB mod non-modded motors. I took the motor apart to find that my motor has had no changes to any ports or the crank when compared to a stock Extech.
What a rip! Someone didn't do their job !!!:flaming::flaming::flaming::flaming: |
could be the EB mods checked all around /runned-in version
which is not bad.. |
Originally Posted by 05tuonojoe
(Post 5951521)
I found out today that I ended up with one of the EB mod non-modded motors. I took the motor apart to find that my motor has had no changes to any ports or the crank when compared to a stock Extech.
What a rip! Someone didn't do their job !!!:flaming::flaming::flaming::flaming: Now if you paid for the full mod motor...$299.00 I'd be smokin mad also..... |
Well Well Well
The saga comes to a close. If have read some of posts then know that I have been through hell and back since nearly day 1. With the help of a good guy from the track and a pro driver my problems are over for now. I turned over all of my rc stuff for some good old wrenching from people who know what they are doing. The problem. Ramping Putty. It came loose from the crank and turned to soft rubber clogging the entire exhaust. I havent ran it yet but they said its a beast now. It only took a month but thank god its over. Not sure what cuased it other 5 drops of after run oil one time when it was brand new and had never been turned over. |
Originally Posted by dishsoap
(Post 5956805)
The problem. Ramping Putty. It came loose from the crank and turned to soft rubber clogging the entire exhaust. I havent ran it yet but they said its a beast now.
It only took a month but thank god its over. Not sure what cuased it other 5 drops of after run oil one time when it was brand new and had never been turned over. |
Hey dish, not to say I told you so.....but that's exactly one of the things I told you to look for 3 weeks ago (page 10, post #1590) Glad you got it figured out though. What did they do, just remove the rest of the silicone and rebuild it without any ramping? I ask because that is what I did, and the engine still isn't right. Could be just way off tune now that the primary flow has changed. LMK, thanks!
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I also don't mean to say i told you so , but i also said the same thing 3 weeks ago. Oh well glad you got it fixed , i've seen many do it.
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So afterrun oil is a no no with these engines?
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Originally Posted by t4ftracer
(Post 5959453)
Hey dish, not to say I told you so.....but that's exactly one of the things I told you to look for 3 weeks ago (page 10, post #1590) Glad you got it figured out though. What did they do, just remove the rest of the silicone and rebuild it without any ramping? I ask because that is what I did, and the engine still isn't right. Could be just way off tune now that the primary flow has changed. LMK, thanks!
Originally Posted by romax
(Post 5959524)
I also don't mean to say i told you so , but i also said the same thing 3 weeks ago. Oh well glad you got it fixed , i've seen many do it.
Yes and Yest. You guys told me so. I am just not skilled enough to tear apart an engine and put back together or what to look for. This is why I dropped it off to someone who knew what they were doing. They ran 3 full tanks through after tunning it and it runs like a champ now. I hope it continues. Going racing tomorrow so we will see. |
Originally Posted by LVBaja
(Post 5960658)
So afterrun oil is a no no with these engines?
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So is the best solution to just run it without any epoxy?
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Originally Posted by t4ftracer
(Post 5962903)
So is the best solution to just run it without any epoxy?
At this moment I will not be sending it away to have it refilled. To me its not worth the headache. Plus I ran a 7 minute B and had over a half tank left!!!!! |
Just remember the epoxy also works as a crank balance..the engine was designed to have the putty in it..I have no clue about what the long term effects would be to remove it, but maybe someone from Sirio or Trinity can chime in, or an pro engine guy. I would like to know what the major differences would be, other than longer run times and a more balanced crank
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