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Old 12-31-1969, 04:00 PM
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Tekno RC EB48.4 Thread

Old 12-31-1969, 04:00 PM
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Old 01-12-2017 | 10:47 AM
  #196  
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As far as I can see there is no difference between the two chainsaw files show. Both are 5/32" or .1526" (3.87604mm) the #19 drill is .166" (or 4.2164mm)....so the chainsaw files are smaller by .010" or so. The #19 drill bit cleaned out more plastic than I would have thought. I tried to put the pins in after having run the drill in forward only...they went through but had a few snags. Once I ran the drill backwards....they fell right through.

Last edited by Flippin 416; 01-12-2017 at 11:02 AM.
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Old 01-12-2017 | 10:51 AM
  #197  
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Originally Posted by Cain
If I am reading this right, it looks like the chainsaw file is smaller in diameter than the #19 bit.

Of the two options, which is better?

I have a reamer but it does take a bit to work it through. To be honest, still kind of surprised that this is still something that needs to be done on version 4 of the buggy.

Lastly, what is the diff between the one referenced and this one:

https://www.amazon.com/Oregon-32-Inc.../dp/B000IC26XE
I agree. You spend $550 on an item and you have to modify it out of the box ? It's 2017 and they can't have a perfect fit for the hinge pins right out of the factory?
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Old 01-12-2017 | 11:15 AM
  #198  
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Originally Posted by suzukipro
I copied this from an excel spreadsheet so the format is bit off, but it shows the FDR using 15 - 21 Tooth pinions for the EB48.1-3 and for the new gearing used in the EB48.4.

TEKNO FDR EB48-.3
Pinion - FDR
15 - 11.73333333
16 - 11
17 - 10.35294118
18 - 9.777777778
19 - 9.263157895
20 - 8.8
21 - 8.380952381
TEKNO FDR EB48-.4
Pinion - FDR
15 - 9.768
16 - 9.1575
17 - 8.618823529
18 - 8.14
19 - 7.711578947
20 - 7.326
21 - 6.977142857
I was using a 17t pinion on my .3 and dropped to a 15t on my .4 and my temps were a bit out of control 160deg with a heatsink and a fan on it.
My motor is a T8i 1950kv. Hoping I can fit a 14t, it should bring the FDR back to the same as my .3 was.
This got me to thinking, what is the benefit of the new ring/pinion ratio if I am gearing it to the same FDR anyway? thanks.

Edit: Also I noticed the new body fits a lot tighter around the front and back. so there is less air getting into and out of the car, this may be a big factor in my motor temps.
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Old 01-12-2017 | 11:24 AM
  #199  
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I agree, but most parts that are molded shift as they cool so there will be binding. Hand fitting parts on the initial build is just part of the challenge of building a great handling rig. I enjoy it most of the time as long as the entire kit doesn't need an X-Acto Knife trim or file job.
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Old 01-12-2017 | 11:33 AM
  #200  
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Originally Posted by jmcelroy42
I was using a 17t pinion on my .3 and dropped to a 15t on my .4 and my temps were a bit out of control 160deg with a heatsink and a fan on it.
My motor is a T8i 1950kv. Hoping I can fit a 14t, it should bring the FDR back to the same as my .3 was.
This got me to thinking, what is the benefit of the new ring/pinion ratio if I am gearing it to the same FDR anyway? thanks.

Edit: Also I noticed the new body fits a lot tighter around the front and back. so there is less air getting into and out of the car, this may be a big factor in my motor temps.

14T FDR = 10.46571428571429
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Old 01-12-2017 | 11:36 AM
  #201  
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Joe have you put your .4 on a scale yet? I'd vent the body and see if you can shed a few grams if possible.
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Old 01-12-2017 | 11:42 AM
  #202  
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The drill bit info would be great to have on the first page.
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Old 01-12-2017 | 12:07 PM
  #203  
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I went to Menards on my lunch break and got a 5/32 chainsaw file. Buzzed it through the arm, and it was still tight. So I buzzed it with a little pressure, up, down, left, right and it was perfect. Then cleaned it out with the reamer. Worked like a charm. Thanks for the suggestion.
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Old 01-12-2017 | 12:13 PM
  #204  
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Originally Posted by greener74
I went to Menards on my lunch break and got a 5/32 chainsaw file. Buzzed it through the arm, and it was still tight. So I buzzed it with a little pressure, up, down, left, right and it was perfect. Then cleaned it out with the reamer. Worked like a charm. Thanks for the suggestion.
As they say, there is more than 1 way to skin a cat.

Either way, glad that you got it just the way you want it.
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Old 01-12-2017 | 12:15 PM
  #205  
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Originally Posted by suzukipro
Joe have you put your .4 on a scale yet? I'd vent the body and see if you can shed a few grams if possible.
No I have not weighed the new one yet. I will have to do that.
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Old 01-12-2017 | 12:48 PM
  #206  
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Originally Posted by Cain
If I am reading this right, it looks like the chainsaw file is smaller in diameter than the #19 bit.

Of the two options, which is better?

I have a reamer but it does take a bit to work it through. To be honest, still kind of surprised that this is still something that needs to be done on version 4 of the buggy.

Lastly, what is the diff between the one referenced and this one:

https://www.amazon.com/Oregon-32-Inc.../dp/B000IC26XE
I had good results with the #19 bit but I can see how the chainsaw files might make for a cleaner hole since it is essentially smoothing out the barrel as it works.

Whereas It took a little finesse to get a clean hole with the #19 bit
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Old 01-12-2017 | 01:14 PM
  #207  
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Originally Posted by jmcelroy42
No I have not weighed the new one yet. I will have to do that.
Also, try your old body on the new kit, to eliminate that entirely from the heat equation. You will need to open the front of the old body up a little for the new ackerman though. I'm also going to be trying to fit a 14t, but for my 2100kv SMC motor.

As for the reason, this all spins the center shaft less quickly, which means the rotating mass down the center is less of a drag on the motor, and therefor more efficient if the rest of the system is the same in efficiency as before.

Last edited by justpoet; 01-12-2017 at 01:28 PM.
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Old 01-12-2017 | 03:16 PM
  #208  
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very curious to see how the temp thing goes with these changes, especially with people running on smaller tracks relative to Kv on a motor.

It may be we are going to want to start sourcing 1700kv motors here ...
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Old 01-12-2017 | 03:40 PM
  #209  
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Hello Cain,
To obtain the highest durability we chose 100% nylon on the arms and unfortunately the shrink rate with this material is somewhat high. We worked with manufacturing to try to eliminate the need for reaming and could not come up with a solution.

Glass filled arms (that many other manufacturers use) require less reaming but are not as durable. Hopefully, the increased durability outweighs the need to ream the arms.

I personally use the chainsaw file with a drill, others like the hudy reamer or the #19 drill bit. It's mostly personal preference. 5/32 chainsaw file is 3.97mm and slightly smaller than the 4.0mm hinge pin. Recommend moving the arm around a little while using the file with a drill. This will help enlarge the hinge pin hole slightly. Goal is to enlarge the hole just enough for the hinge pin to fall through by gravity (and maybe a slight tap) alone. Reaming it too far will cause excessive slop in the suspension.

Originally Posted by Cain
If I am reading this right, it looks like the chainsaw file is smaller in diameter than the #19 bit.

Of the two options, which is better?

I have a reamer but it does take a bit to work it through. To be honest, still kind of surprised that this is still something that needs to be done on version 4 of the buggy.

Lastly, what is the diff between the one referenced and this one:

https://www.amazon.com/Oregon-32-Inc.../dp/B000IC26XE
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Old 01-12-2017 | 03:47 PM
  #210  
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Hello Jmcelroy42,
I might have missed it but what are the dimensions of the track you run on? 17t on the .3 and 15 on the .4 is quite low gearing. Meaning it should be running this gearing on a very small track. If you are running on a larger track, we recommend going to a larger pinion as 4 pole motors can generate excessive heat if the RPMs are too high. We pretty much run 16 or 17 on all tracks with a T8 1900.

Also, a T8i might not be the best motor if you are running into heat issues. you might need to be using a T8.

Another issue could be the motor is old. Over time the magnets lose their strength causing you to push the motor harder, generating more heat.

165 degrees F is not excessively hot and you should be fine as long as temps do not go over 200 too regularly. I've seen Tekins go up to 300 and still be fine.

Originally Posted by jmcelroy42
I was using a 17t pinion on my .3 and dropped to a 15t on my .4 and my temps were a bit out of control 160deg with a heatsink and a fan on it.
My motor is a T8i 1950kv. Hoping I can fit a 14t, it should bring the FDR back to the same as my .3 was.
This got me to thinking, what is the benefit of the new ring/pinion ratio if I am gearing it to the same FDR anyway? thanks.

Edit: Also I noticed the new body fits a lot tighter around the front and back. so there is less air getting into and out of the car, this may be a big factor in my motor temps.
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