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Do I need a pinch?
:lol::lol::lol::lol::lol::lol::lol::lol::lol::lol: :lol::lol:
My friends losi rtr .27 engine, we wondered why it wouldnt run well, sending it out for a sleeve resizing lol http://i23.photobucket.com/albums/b3.../photo-1-1.jpg |
Yea I would say its getting close to needing a pinch. It wouldn't hurt to go ahead and do it now. lol
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Not getting close. That definitely needs a pinch... The piston shouldn't come up through the sleeve.
Who'd you send it to? |
getting close ,,,, i would say way past due thats me
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since rcrenew dosent work on these size sleeves im sending it to rayaracing
i dont even know how this thing honestly ran after seeing this, never seen a p/s get this bad |
i can tell you just from looking at it, that it has been run incredibly lean
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Definitively need a pinch... or a new piston and sleeve
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Originally Posted by anthonys88
(Post 8067213)
:lol::lol::lol::lol::lol::lol::lol::lol::lol::lol: :lol::lol:
My friends losi rtr .27 engine, wondered why it wouldnt run well, sending it out for a sleeve resizing lol http://i23.photobucket.com/albums/b3.../photo-1-1.jpg |
well actually it does look alittle LEAN :lol::lol::lol:PINCH IT AND RUN IT
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WOW yeah time for www.rayaracing.com they are the best out there
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I have never seen a P/S like that hahahahahahhah
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please, this is not my p/s, but out of a friends losi rtr .27 mach engine. its near 3 years old now. i sent my v-spec p/s to rayaracing along with this, i hope he can get the .27 back into spec. it would actually run for about a tank pretty well.
today we were at the track and i clocked it at 240 degrees but it still showed a nice smoke cloud, i richened it up a bit and it would bog so bad lol. after the one tank he tried to go for another but couldnt get it re-started, so i looked at it and i was like wtf is the glow plug out? the motor had what felt like no compression, to which i then learned that it actually didnt, so i took it apart and sent it to ray, we'll see lol |
Originally Posted by dreaux
(Post 8067339)
i can tell you just from looking at it, that it has been run incredibly lean
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piston looks fine to me. If your assuming its lean because there is no carbon on the piston, well, that just means he is running good fuel and not running the motor slobbering rich...
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Originally Posted by hdcruzer
(Post 8067926)
Id say you dont know what your looking at. The only thing wrong with that piston and sleeve is it needs a repinch. If he hasnt cleaned the top of that piston, and thats the way it came out, is the reason that motor has run as long as it has. Arent you the one that has gone through a ton of motors and always had problems tuning them??????? Maybe if you knew what you were looking at youd have better luck......
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Originally Posted by rodcpierce
(Post 8067940)
piston looks fine to me. If your assuming its lean because there is no carbon on the piston, well, that just means he is running good fuel and not running the motor slobbering rich...
and it has been eating glow plugs, like 1 every 10 tanks or so |
Ohh just some FYI the Mach 427 is actually a .26! The 427 on the side is simply .427 cc which comes out to .26 ci ! :nod: but yeah I'm surprised it actually still ran with that pinch!
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Originally Posted by Jomo918
(Post 8068594)
Ohh just some FYI the Mach 427 is actually a .26! The 427 on the side is simply .427 cc which comes out to .26 ci ! :nod: but yeah I'm surprised it actually still ran with that pinch!
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Needing a Pinch
Hmm. I don't think that's right.
The piston has gone a little too far. I think you need to get that fixed. Time to get the sleeve pinched. |
got everything back, ray did an awesome job, the motor ran awesome also
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Very nice. Did you have to rebreak-in at all?
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Originally Posted by quixoticboi
(Post 8103999)
Very nice. Did you have to rebreak-in at all?
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