New to this forum, New to RC off road, so this may be a novice Question!!
I have built a Scorion AX10 and placed a Novak brushless GoatCrawler with electronic speed controller. Radio is a Futaba Magnum 2 PL FM unit.
PROBLEM- when running the truck (especially in reverse) it jumps back and forth like there is radio bleed through/controller is screwy. This has happened at home, at our house in Smithville and my office in Columbia.
I adjusted the throttle stops/sets per the Novak directions. Steering is no problem and the truck USUALLY responds with no issues.
ANY IDEAS WOULD BE GREATLY APPRECIATED!!!!!